Is there some weird setting in the firmware for this, or is this just something to do with the SKR Mini E3 V3 that I installed? It's not causing problems per se, it's just. ![]() It does this for auto homing as well as when using bilinear bed leveling. But when it gets close to the final target, (easily <10 mm away, perhaps just a few mm), it'll slow to an absolute crawl, like maybe 1 mm/s of carriage movement in both the x and y axis - and it'll just take it's time to finish the move. To reiterate - if I'm doing an auto home with Marlin, the bulk of the movements will be INSANELY fast with a very high acceleration/jerk value to start with.
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